Sunday, November 10, 2019
Monday, November 4, 2019
Finished? For now anyway...
I wrapped up post-paint tasks over the past few days including:
- re-inspection of all bolts, jam nuts (none of these were loosened by the paint shop but I checked them anyway), cotter pins, and miscellaneous hardware installed at the paint shop.
- installation of fairings
- installation of the full interior. I had previously only been using the front carpets.
- installation of a snubber for the manifold pressure gauge. I had been seeing some vacillation in MAP values and this solution is apparently recommended by Garmin to damp the readings.
- drained all fuel from aircraft and re-weighed. Gained about 23 pounds from the paint.
- rechecked and adjusted nose wheel break out force. I noticed after paint that it felt a bit loose. I removed the bellville washers, cleaned and greased them while I had the cotter pin out.
Random note: before I took N14VB to the paint shop, I was never fully happy with the elevator friction. While in the paint shop, I made some new shims for the center bolts using stainless steel sheet material. I had used feeler gauges to get as close as possible on the extra width needed and there were no standard washers that would fit. I'm very happy with the result - the elevator friction is about as low as I can imagine it being now.
Sunday, October 27, 2019
Tuesday, October 22, 2019
Monday, October 14, 2019
Friday, October 11, 2019
Friday, October 4, 2019
In the paint shop
Last week I finally got N14VB to the paint shop. I chose Ormond Aircraft in Ormond Beach, FL. Close to where I live and recommended by several folks I know including one RV on my field and a local flight school (Holladay Aviation at KCRG) which has several aircraft painted by them.
Surface prep - acid wash/alodine/scuff and high-build primer on fiberglass part:
First coat of paint:
Surface prep - acid wash/alodine/scuff and high-build primer on fiberglass part:
Epoxy primer:
First coat of paint:
Monday, August 19, 2019
FWF inspection
I pulled the cowling today and inspected the FWF area. Not the first time I've done this but I was being very thorough. Found a couple of minor issues:
1. Slightly loose bolts (castle nut style) on throttle and mixture cable rod ends. Tightened these until snug and put in new cotter pins. I reversed the mixture cable bolt and used a shorter one because there was slight wear on the lower cowling from rubbing at full rich mixture setting.
2. Broken L-bracket for the sniffle line. This bracket clamps to the exhaust using a stainless hose clamp, with an Adel clamp holding the sniffle line. Looks like heat and flexing broke it at the bend.
I fabricated a new one using .018 stainless steel. Hopefully this will be more durable.
Broken bracket and new one fabricated from steel:
1. Slightly loose bolts (castle nut style) on throttle and mixture cable rod ends. Tightened these until snug and put in new cotter pins. I reversed the mixture cable bolt and used a shorter one because there was slight wear on the lower cowling from rubbing at full rich mixture setting.
2. Broken L-bracket for the sniffle line. This bracket clamps to the exhaust using a stainless hose clamp, with an Adel clamp holding the sniffle line. Looks like heat and flexing broke it at the bend.
I fabricated a new one using .018 stainless steel. Hopefully this will be more durable.
Broken bracket and new one fabricated from steel:
Thursday, August 8, 2019
Out of Phase 1.
I completed phase 1 a few days ago (see screenshot below - happened to grab a screenshot at the exact magic time).
Still tweaking stuff - need some engine data to tweak fuel injection nozzles. I'd like the engine to run more smoothly lean of peak and so far two cylinders (1 and 4) seem to be leaner than the other two. Don at Airflow Performance is looking for some detailed data to help tweak this.
Also planning to get paint done very soon.
Ignore the oil temp - it goes up a bit in a climb but settles right down, I haven't seen it over about 210 or so.
Still tweaking stuff - need some engine data to tweak fuel injection nozzles. I'd like the engine to run more smoothly lean of peak and so far two cylinders (1 and 4) seem to be leaner than the other two. Don at Airflow Performance is looking for some detailed data to help tweak this.
Also planning to get paint done very soon.
Ignore the oil temp - it goes up a bit in a climb but settles right down, I haven't seen it over about 210 or so.
Sunday, May 12, 2019
She's FAST!
Totally consistent with Van's promised performance, with wheel pants/fairings now on, I'm seeing outstanding performance numbers, at slightly lower power settings than expected.
Pants/fairings added 18-19 knots to speed. I had added a rudder wedge but had to remove it as the faster speeds magnified its effect: I still need to hold a small amount of right rudder in cruise. I need to decide whether to use a cut-down wedge, a small tab, or an internal rudder trim. I'm tempted to add an electric trim tab like many RV-10 owners have done, but wonder if the effort is worth it.
I have a consistently heavy right wing - I think the left flap quick build) has a slight twist. I'm going to build a new left flap and install it before I chase down the heavy wing issue any further.
Wig wag and another landing videos:
Pants/fairings added 18-19 knots to speed. I had added a rudder wedge but had to remove it as the faster speeds magnified its effect: I still need to hold a small amount of right rudder in cruise. I need to decide whether to use a cut-down wedge, a small tab, or an internal rudder trim. I'm tempted to add an electric trim tab like many RV-10 owners have done, but wonder if the effort is worth it.
I have a consistently heavy right wing - I think the left flap quick build) has a slight twist. I'm going to build a new left flap and install it before I chase down the heavy wing issue any further.
Wig wag and another landing videos:
Wednesday, April 24, 2019
Transitioning into Phase 1 - flying for real
Since last post I've spend quite a bit of time fixing and tweaking issues found on first flight and re-checking a whole lot of stuff. This includes fixing the trim issue by replacing the micro-molex connector in the empennage for trim with a much better Deutsch DTM connector. This will make it a bit harder to remove elevator but I'll figure that out when the time comes (most likely will add another connector where trim wires are currently secured with dsub pins/shrink wrap).
I also fixed issue with ADAHRS alignment (my bad - configured it wrong), re-calibrated the ADAHRS and magnetometer, and spent a lot of time checking MAP connections and possible leak sites. Also pulled and cleaned spark plugs and checked fuel/oil fittings, wiring, etc. Looking for any leaks, loose fittings, etc. All look good.
I've flown twice (total 3.1 hours) since first flight, focusing mostly on getting the feel for the airplane, running the engine hard, and testing various systems in flight. One issue that will require a future fix is the standby alternator - it correctly detects when primary is offline but voltage doesn't come up so for some reason it's not producing voltage. I'll call B&C when I have some time to help with troubleshooting.
I noticed the right wing is heavy, also I need pretty much constant right rudder to keep the ball centered. I noticed in level light that the right aileron is a bit higher than my original setting - I had set it using wingtip and the alignment jig, and noticed that it sat about 1/4" higher than the inboard flap. I thought this indicated a twist in the flap but now I think the aileron was adjusted a bit too high, so I adjusted the control rod to bring it closer to the flap. We'll see how that feels next flight. Once I get the heavy wing issue resolved, I'll reassess the rudder and add some trim as needed (trim tab or similar). These are normal, expected issues.
I've been using/testing autopilot - I set it up with recommended values for the -14A and it's working perfectly. Makes it easier to evaluate issues in flight. Will activate auto trim for the next flight.
The airplane flies very nicely and I'm surprised how fast it is with no fairings in place. I'm seeing about 150 knots at lower altitudes so with fairings and higher up won't be surprised to see 170 knots plus - I hope.
Improved connector for trim in empennage:
Screenshot from today's flight. Autopilot doing the hard work!
I also fixed issue with ADAHRS alignment (my bad - configured it wrong), re-calibrated the ADAHRS and magnetometer, and spent a lot of time checking MAP connections and possible leak sites. Also pulled and cleaned spark plugs and checked fuel/oil fittings, wiring, etc. Looking for any leaks, loose fittings, etc. All look good.
I've flown twice (total 3.1 hours) since first flight, focusing mostly on getting the feel for the airplane, running the engine hard, and testing various systems in flight. One issue that will require a future fix is the standby alternator - it correctly detects when primary is offline but voltage doesn't come up so for some reason it's not producing voltage. I'll call B&C when I have some time to help with troubleshooting.
I noticed the right wing is heavy, also I need pretty much constant right rudder to keep the ball centered. I noticed in level light that the right aileron is a bit higher than my original setting - I had set it using wingtip and the alignment jig, and noticed that it sat about 1/4" higher than the inboard flap. I thought this indicated a twist in the flap but now I think the aileron was adjusted a bit too high, so I adjusted the control rod to bring it closer to the flap. We'll see how that feels next flight. Once I get the heavy wing issue resolved, I'll reassess the rudder and add some trim as needed (trim tab or similar). These are normal, expected issues.
I've been using/testing autopilot - I set it up with recommended values for the -14A and it's working perfectly. Makes it easier to evaluate issues in flight. Will activate auto trim for the next flight.
The airplane flies very nicely and I'm surprised how fast it is with no fairings in place. I'm seeing about 150 knots at lower altitudes so with fairings and higher up won't be surprised to see 170 knots plus - I hope.
Improved connector for trim in empennage:
Screenshot from today's flight. Autopilot doing the hard work!
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